It does make a difference, but opening up the throttle a bit gets it into a surging, lopside chug that belches raw fuel out the exhaust as vapor-you can literally light the exhaust on fire with a lighter. BIG boom after it's "idled" a minute! Opening the throttle too much causes a rapid RPM surge then it stalls out lean. Never does foul out the plugs-just soaks them in fuel. Gotta hand it to the GM DIS coil packs-they're blasting away like a champ.
I have some time this evening, so I plan to go back out to the combustion lab and see what I can do as far as getting the idle straightened out and try the capacitor trick-it may be something as simple as trying to pull switched power from the wrong place, too, so who knows what I'll end up having to do to fix it yet.
Found a bad relay contact in the switched ignition line-was dropping 2.5V across the contact. This made a significant difference, but still hasn't fixed the massive amount of data corruption on the ALDL line-but at least it's talking now.
So I've made another terrible video for Youtube, to try and explain better what's happening here. I still don't have a clue what's going on, maybe VATS is killing it, maybe it's super rich, I can't tell.
The wideband shows 13-14 AFR's when it starts, but when it would normally shift to the running table, I can't tell what happens because the engine either stalls out and dies, or I have to pedal the crap out of it to try to keep it running. The datastream is wigging out the whole time too, at least I have a datastream. Unfortunately, I haven't kept it running long enough to accurately measure the *running* PCM voltage. I still don't think it's an issue, though, because swapping to unpatched stock code and a 1 bar sensor lets the truck idle and free-rev OK, as long as I've changed the injector flow constant and the blower is bypassed.
Fixing the voltage issue did solve the super-rich chugging issue where it would fill the whole lab with fuel vapor, though! Gotta take a win where I can get one.
https://www.youtube.com/watch?v=nrXr...ature=youtu.be
There's a video of last night's work-I am building a little VATS module to test and see if that's the issue. Who knows, it's ten minutes to get one going.
Possibly another update tonight.
89 K1500 Scottsdale 5.7L 5spd 3:42 RamJet cam Dart iron TBI heads 427 PCM swap
95 C2500 Cheyenne 6.5L turbo diesel 4L80e 4:10 DB2-4911 Manual pump conversion 0411 PCM trans control 2Bar COS
05 Outback XT 2.5L turbo gas auto
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